阿拉斯加 737 Max 飞行中舱门爆裂后驾驶舱数据被删除
Alaska 737 Max Cockpit Data Erased After Mid-Flight Door Blowout

原始链接: https://www.zerohedge.com/markets/alaska-737-max-cockpit-recording-data-erased-after-mid-flight-door-blowout

上周,阿拉斯加航空的一架波音 737 MAX 9 飞机在波特兰附近飞行期间突然减压,由于未能在两小时限制之前激活保存录音的断路器,导致驾驶舱的关键数据被删除。 美国国家运输安全委员会主席 Jennifer Homendy 分享了这一消息,并表示不会恢复任何数据来帮助解释导致机身面板在 16,000 英尺高度从飞机上脱落的事件发生的原因。 这一不幸的损失发生之际,人们呼吁改变有关记录时间的规定,以提高航空安全标准。 此前涉及 MAX 系列的事件凸显了对其主要制造商波音公司及其主要供应商 Spirit AeroSystems 的设计和生产质量的担忧。 在机场外发现的新一代 iPhone 也为这一事件提供了一些线索,但鉴于事件的意外性质,其功能仍不确定。 因此,围绕这些场景中主要参与者的责任和罪责仍然存在疑问。

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原文

National Transportation Safety Board (NTSB) chair Jennifer Homendy said cockpit recording data on the Alaska Airlines Boeing 737 MAX 9 jet, which lost a fuselage panel that triggered a sudden decompression event near Portland on Friday, won't be retrieved because the data was erased. 

On Sunday, Homendy told reporters that after Alaska Airlines Flight 1282 made an emergency landing at Portland International Airport - the ground crew did not pull the circuit breaker on the cockpit voice recorder, or black box, to preserve the audio, which only holds two hours or data, as required by federal law. 

"There was a lot going on, on the flight deck and on the plane. It's a very chaotic event. The circuit breaker for the CVR (cockpit voice recorder) was not pulled. The maintenance team went out to get it, but it was right at about the two-hour mark," Homendy said.

She continued: "The cockpit voice recorder was completely overwritten. There was nothing on the cockpit voice recorder." 

Reuters noted US cockpit recorders only need to log two hours of data versus 25 hours in Europe for aircraft made after 2021. 

The NTSB head said the audio could have shed more light on the moments leading up to the aircraft's door ripping off the fuselage at 16,000 feet. 

Homendy called on the "FAA to change the rulemaking" on cockpit recorders, extending the recording time from 2 to 25 hours for all aircraft.

"If that communication is not recorded, that is unfortunately a loss for us and a loss for the FAA and a loss for safety because that information is key not just for our investigation but for improving aviation safety," she said.

During the decompression event, a new-generation Apple iPhone was sucked out of the plane and landed near a road in Portland. An X user named "Seanathan Bates" discovered the device, which did not appear to be damaged. 

In a separate report, Bloomberg Intelligence's George Ferguson and Melissa Balzano believe the in-flight mishap "probably stems from a manufacturing oversight, a sign of deficiency at Spirit AeroSystems, Boeing's key supplier." 

Don't forget the Max program is a flying disaster. 

The FAA has previously rejected the NTSB's call to upgrade aircraft with new cockpit voice recorders. That should be reversed since Max jets "designed by clowns who in turn are supervised by monkeys' continue to fly around. 

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