驾驶员起诉波音公司,称公司不公平地将其责怪,此前他曾成功着陆一架面板脱落的飞机。
Pilot Who Landed Plane After Panel Blew Out Sues Boeing, Claims Company Unfairly Blamed Him

原始链接: https://www.zerohedge.com/political/pilot-who-landed-plane-after-panel-blew-out-sues-boeing-claims-company-unfairly-blamed

阿拉斯加航空机长布兰登·费舍尔因安全降落2024年1月因机舱门塞子脱落的1282航班而被誉为英雄,现在正在起诉波音公司。尽管最初获得了包括联邦航空管理局和国家运输安全委员会在内的官员的赞扬,但费舍尔指控波音公司试图通过暗示不当维护或误用,来转移对事故的责任——该事故是由制造过程中缺少螺栓引起的。 据费舍尔的律师称,这导致乘客对他提起了诉讼,给他造成了极大的困扰。国家运输安全委员会的调查证实了制造缺陷,并赞扬了机组人员对紧急情况的处理。据报道,波音工厂的工人感到被迫快速工作,并在没有充分培训的情况下执行任务。 费舍尔感到个人被背叛,他一生都在驾驶波音飞机,并认为波音公司试图将他作为替罪羊与他们声称对飞行员的尊重相矛盾。这起事件导致八人轻伤,并凸显了波音生产过程中严重的质量控制问题。

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原文

An Alaska Airlines pilot who was universally praised as a hero after safely landing a Boeing jet after a door plug panel flew off shortly after takeoff is suing the company because he says the plane maker wrongly tried to blame him and the rest of the crew.

The section of a Boeing 737 Max where a door plug fell while Alaska Airlines Flight 1282 was in flight on Jan. 7, 2024. NTSB via AP

Captainn Brandon Fisher received accolades from the heads of the National Transportation Safety Board and the FAA, along with some Boeing executives, when he safely landed flight 1282 in January 2024 with 177 people on board. 

According to Fisher's lawyers, however, Boeing's attempts to deflect liability in past lawsuits caused some passengers to sue the pilot, causing him great distress, AP reports. Four flight attendants previously sued Boeing over the incident last summer.

Fisher claims that Boeing suggested it wasn't responsible because the plane was 'improperly maintained or misused' by others.

"It was clear Boeing’s words were directed at Captain Fisher in attempt to paint him as the scapegoat for Boeing’s numerous failures," his lawyers, William Walsh and Richard Mummolo wrote in their lawsuit filed in an Oregon court.

Bolts Were Missing

An NTSB investigation of the incident revealed that four bolts securing what is known as the door plug panel were removed and never replaced during a repair on the Boeing 737 Max 9 aircraft while it was being assembled. Both Boeing and Spirit Aerosystems - which has since been acquired by Boeing, were both implicated. 

The bolts in question are hidden behind interior panels on the plane, so they aren't something that could have been easily checked in a preflight inspection by the pilot or anyone else from the airline (i.e. Boeing's assembly line was responsible). NTSB investigators concluded that the door plug was gradually moving upward over the plane's 154 flights prior to the incident before ultimately flying off.

"Boeing’s lie infuriated Captain Fisher as well, as he was being castigated for his actions as opposed to being lauded," wrote Fisher's attorneys. "Because he had flown Boeing aircraft for the entirety of his employment with Alaska Airlines, Boeing’s attempts to blame him felt like a deep, personal betrayal by a company that claimed to hold pilots in the highest regard."

The NTSB was unequivocal in its determination that this was a manufacturing issue, and the crew's actions were exemplary

The Blowout

The incident occurred minutes after the flight took off from Portland, Oregon - creating a significant air vacuum in the cabin. Seven passengers and a flight attendant sustained minor injuries, but Fisher was able to land the plane safely.

The blowout caused a 2x4 foot piece of fuselage covering an unused emergency exit behind the left wing to be ejected from the plane. 

During the investigation, Boeing factory workers told NTSB investigators that they felt pressured to work too fast, and were asked to perform duties they weren't properly trained for

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